JDL I was a little premature with the answer or should I say the chevy garage! They called me back today and that was not problem! So they called th gm teck line and they told them disconnect convertor on bank 1 to see if the cat was plugged. The tec there who I know was so puzzled at this truck he was ready to burn it to the ground! Being a person who would not give up on a problem looked futher. Well guess what he found? #4 cylinder had a broken exhaust valve spring which was cause'ing a lean code to pcm, mass-air flow! There for adjusting pcm and every thing else, so there was not misfire in #1 and #3 there were firing all along. A simple thing of pulling of a valve cover was all it took to find the problem in which other tecs would have blowen off. Who would of thought that an opposite bank would cause this problem hey? Well I would like to thank you for all your help with my problem and hope you a long time in helping other people with there car-truck problems that's why god put you here to help! Thanks BOB
P.S if you don't hear from me it's fixed! Lol
Friday, March 10th, 2017 AT 3:30 PM
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